Cam Sprocket Puller
brought to you by:  Dave Williams
This page: www.bacomatic.org/~dw/tool/djpuller/djpuller.htm
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Last Updated: 25 Aug 2008
Author: Dave Williams; dlwilliams=aristotle=net
Sometimes it seems I wind up making a lot of tools. In this case, I was
degreeing the cam on a 351 Ford. I drove the sprocket on with my aluminum
pipe, no big deal, checked the phasing, had to pull the sprocket off to move
it a notch.
No way.
That's an aftermarket aluminum block, and that's a 351 Cleveland sprocket, so
there's no room to get any puller jaws back there. I ground down the jaws on
two pullers, but they wound up about .090" thick and simply bent when I tried
to remove the sprocket.
I bought a matched pair of small crowbars, which couldn't get enough leverage
to budge the thing. Then I tried making a puller out of angle iron and bolts.
It simply bent into scrap when I leaned hard on the wrenches. I made another.
No joy there either.
Finally, it was down to taking the angle grinder and destroying a $150
Rollmaster timing set, or, hell, why quit when I'm losing? I already had way
more hours into the project than I could justify. Might as well go for broke.
Here we are, half a day into the project. Fat chunks of 1018 cold-rolled
steel, sawed, milled to size, drilled, and tapped. It's 1-1/4" thick.
Small lathe faceplate. I normally use hardware-store washers on the bolts,
but in this case I made some heavy quarter-inch washers to hold the heavy
puller. Note the offset.
Line it up with the dead center in the tailstock. Then I used an indicator
and the brass hammer to get it closer.
A bunch of drilling and boring, and now the puller is clamped to the gear.
3/8" steel plate and 3/8" fine thread bolts. I put tension on the bolts,
whacked the center of the plate with the brass hammer, and the sprocket would
move a little. Lather, rinse, repeat.
Voila! It's off! Hallelujah! And the SOB fought every bitter millimeter,
too.
...disassemble the bits...
...and there's the gear! Note how thin the flange that actually pulls the
gear is.
I had thought I might need to put some extra bolts or pins in the blocks to
keep them from swiveling when I put tension on the puller, but everything
stayed lined up fine.
The gear looks perfectly normal under the lights in the shop; for some reason
the flash and digital camera make it look like the teeth were formed by rabid
weasels. It is a new gear, other than turning the engine over a few times by
hand to degree the cam.
So, after far more time than I can think about without wincing, the g*****d
gear is off! The crank snout is a hair larger than either of the stock Ford
cranks I have on hand, so I'll polish the crank nose a bit to get a little
less interference.
If the b***h sticks again, Mr. Puller will rip its face off...